Blog

Fuel leak from No.1 ECU traced

Work continued this week:

• Fuel leak from No.1 ECU traced

• Engine removed for access

• Oil scavenge pump gasket changed

• Engine refitted

• Starter generator replaced

• Wet and dry runs carried out to bleed fuel system

• Minor instrument snags rectified

• Torque meter test procedure researched and gauges tested

• Rad alt system tested and new gauges fitted

• Engine and airframe prepped for ground run

• No.1 engine run up to 95% power successfully with no problems

Work to be continued next week:

• Continue major service.

• MODs research.

• AC generation system testing.

• Research DC generation system.

twentytwopl 18 May 2021 Uncategorised

Blog post image
Blog post image
Blog post image

SIGN UP TO OUR NEWSLETTER

Lorem ipsum dolor, sit amet consectetur adipisicing elit. Illo obcaecati accusamus architecto recusandae necessitatibus incidunt quidem nam earum fuga optio cum suscipit quam quas, molestias explicabo voluptatibus officiis dicta minima!